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#21 |
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MM's resident Juice head
07 Mustang GT
Join Date: Nov 2007
Location: PA
Posts: 7,920
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i agree on the cams being tigtened incorectly....also, as soon as you strap your car to the dyno you sign a waver dont you? I know i did
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#22 |
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Hardcore Enthusiast
Join Date: Feb 2009
Posts: 1,462
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I have never signed anything at JPC over the last few years, but that may just be due to having a good relationship with Justin.
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JDM 302 Stroker, Whipple 10 rib 12 psi, L&M, JBA, J&M, LFP, Corsa, BBR Stage II cams, Manley, MGW, McLeod RST, Metco, Steeda, Autometer, CDC, Street Scene, SOS, Tuned at JPC Racing by Kevin MacDonald |
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#23 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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Thanks for all the responses, I'll try to answer all your questions. I did not sign a waiver. They pulled the valve covers in front of me. The exact damage was cracked and out of place rocker arms, some scuffing on the cam shaft (all passenger side), and later, when i was not there he said there were some damage to the valves and some scratches to one piston. I did sign a waiver at the dyno, but that was not the shop that did the cam install. I am consulting a lawyer this week to find out where I stand. I am also going to ask what they torqued the cam bolts to. I heard that a mere 2lb of difference can cause engine failure. Oh, and the heads were pulled and they have been ported and polished.
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#24 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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Almost forgot, after the install on the way to the dyno, the car would stall sometimes at a stand still, and the best that i can describe it is the engine did not like to sit still. After the dyno it ran great, and then boom the engine blew, on the trip back.
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#25 |
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Regular
Join Date: Oct 2007
Posts: 121
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sounds like multiple lash adjusters
had insufficient oil pressure, to keep the cam followers in place. if the broken followers were right next to eachother, then maybe it was just one lash adjuster which had the problem. regardless, sorry it happened to you and i hope it all works out for you in the end. |
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#26 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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yeah I know this situation sucks, but just to clarify I am not blaming the shop. It seems highly likely from what I have heard that it was their fault and at the very least they should accept a neutral standing given the circumstances.
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#27 | |
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Doctor of Jurisprudence
2005 Mustang GT
Join Date: Mar 2007
Location: Republic of Texas
Posts: 2,858
Blog Entries: 1
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I'm confused...you're not blaming them, but it's their fault?SOMEBODY is at fault...here are your choices A) faulty part, B) faulty install, or C) faulty engine. Only one of these choices leads to you paying for everything out of your pocket...don't feel bad about pointing the finger at someone. The way our system works is that the finger is pointed at yourself as being at fault until you start pointing at someone else...better pick one and stick with it brother. (please refer to previous legal disclaimer in this thread)
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#28 |
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MM's resident Juice head
07 Mustang GT
Join Date: Nov 2007
Location: PA
Posts: 7,920
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what was your A/F on the dyno
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![]() The MGW short throw shifter Its not just a shifter...It's a lifestyle! |
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#29 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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A/F Min 12.7
Max 13.7 Avg 13.0
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#30 | |
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Regular
2006 Mustang GT
Join Date: Apr 2007
Location: Spangdahlem Air Base, Germany
Posts: 411
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Don't get me wrong, by no means am I implying that the mechanical defect is your fault...but the car was not running right and still put it on the dyno to run at WOT? That I don't understand.
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11.67 - 1.64 60' @ 119mph Livernois 298ci Stroker, Saleen S/C, GT500 FPs, SD 60# inj, GT500 T/B, Thump Tensioner, BGG 8 Rib, Kooks, Gords HE, 4.10, TrueTrac, Spec 3+, Pro 5.0
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#31 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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The shop that installed the cams told me that the car would run that way until i got the tune from the dyno, and yes the dyno pushed it to 6400 rpm or so. I find that weird since they are mild cams.
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#32 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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Just talked to the owner of the shop and he said that the valve caps were torqued to 89 inch pounds. No way to prove that though. My issue now is would I be able to tell from the car wanting to stall before the tune that the valve caps were too loose??
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#33 |
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Regular
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#34 |
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June 2010 ROTM
2000
Join Date: May 2008
Location: Ft. Lauderdale, FL
Posts: 1,539
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if its an 08 and only 17k miles, can you put it back to stock, have it towed in and get it fixed under warranty?? Just askin...
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HPDE Instructor PCA, HOD, Track Guys, ERME www.RaceCarTowHooks.com My Track Videos http://www.youtube.com/user/Msirlin My Garage page: http://www.moddedmustangs.com/forums...-member-17090/
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#35 |
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Hardcore Enthusiast
Join Date: Feb 2009
Posts: 1,462
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You always come in way later than my car gets strapped on. (worse than banker's hours??) I kind of figure it's my problem if it pops especially when Kevin's tuning and I'm pushing the stock shortblock.
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JDM 302 Stroker, Whipple 10 rib 12 psi, L&M, JBA, J&M, LFP, Corsa, BBR Stage II cams, Manley, MGW, McLeod RST, Metco, Steeda, Autometer, CDC, Street Scene, SOS, Tuned at JPC Racing by Kevin MacDonald |
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#36 |
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Regular
2008 Mustang GT
Join Date: Dec 2007
Location: Dallas, TX
Posts: 55
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Well finally the shop is being responsive. They are going to help me out with part of the labor and the motor is being rebuilt to a forged 302 stroker. Luckily I haven't spend every penny on upgrades, and it makes sense to do a rebuild when the motor is already torn apart. It's a lot of money...I guess its worth it. Thanks for all the help guys. I talked to a lawyer and he said it was a dead end, and it would be really hard to prove anything.
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#37 | |
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More Is Better.
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Roush Short shifter / Carmen's 3.47" TVS pulley Roush TVS Supercharger Steeda suspension /Big Brakes Mac L/T's / Prochamber / Roush Extremes KB BAP "Daily Driver" RWHP: 492@9 PSI w/ LT's "Dyno Queen": 512@12 PSI-stock exhaust Mods in Garage |
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#38 |
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Enthusiast
Join Date: Oct 2009
Posts: 527
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Wow this situation really sucks
I honestly hope everything works out for the better for you. Don't give up, if it is really their fault, fight till the end.
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