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#1 |
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Hardcore Enthusiast
1989 Mustang GT 5.0
Join Date: Oct 2007
Location: CT
Posts: 2,186
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Foxey Lady is tuned (93Hatch step into my office)
ok so here is the latest update,
baseline stock dyno 191hp 253 trq bolt ons 213hp 268 trq tonight, heads/intake/tb/turbo 1st pull 440hp 620trq 2nd pull 504hp 647trq 17lbs of boost (omg! im so happy she held together) my 38mm wastegate is not big enough, going to swap for a tial 44mm 3rd pull 520hp, had to cut her off early due to drop of fuel pressure... tuner was letting off at 6k he said she wanted more (no need)CAR IS A MONSTER, i did not expect so much power and torque, crazy....where are some z06's lol ill post up dyno sheet soon, gotta take a pic of it, driving on hwy she spiked to 20lbs of boost and HELD up! crazy but im going to get a 10lb wastegate spring, cuz i do not want to break anything absolute madness! stock bottom end, stock block, stock cam, 93 pump gas
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Cage Maximum Motorsports Sparco QH/BE Nitto "a huge bad azz motor is nice untill you have to turn or stop" |
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#2 |
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I Post Entirely Way Too Much
1993 5.ohhhh
12.97 @140mph
Join Date: Apr 2006
Location: Gatorland
Posts: 6,122
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Dude, you've prob already put a crack smewhere in your block from doing that more than once. Keep it to the first pulls numbers and you will be fine, but 20lbs, no no.
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02 Pewter z28, hoosiers/lid/exhaust/spray...125mph 1993 gt Sold, already missed ![]() --Moates Quarter horse $225-- --Cobra intake $150-- --tremec 3550 bell and shifter $1100--
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#3 |
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Hardcore Enthusiast
'89 LX 'Vert
10's or bust... Literally.
Join Date: May 2009
Location: Denver, Co
Posts: 2,915
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lmao @ 20lbs
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H/C/I 302 + nitrous for now... supercharger/turbo soon? ![]() |
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#4 |
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Banned
1992 Lx
11.39@119.24
Join Date: Jan 2008
Location: Az
Posts: 11,644
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kits a piece of shit if it keeps creepin boost that bad dude, did you get it tuned with no waste gate spring? luzlz
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[QUOTE=93mustank;2577445]We speed tested my right arm for quickness in shifts... So he could design the cam for proper shift recovery.[/QUOTE] |
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#5 |
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Premium Member
1969 Mustang Mach 1
6.824@101.61
Join Date: Aug 2006
Location: Oklahoma jackass, get to driving
Posts: 5,565
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Tick.....tick........tick......tick..........
Be careful with that thing, or you'll be doing it again.
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./___ _ ____ ___ \. ( ]]] _ _ O _ _ [[[ ) \_ o _ _____ _ o _/ |___| ......... |___| http://www.youtube.com/watch?v=HyYU3...e_gdata_player |
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#6 |
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Regular
Join Date: Mar 2011
Location: Dayton, Ohio
Posts: 181
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Wow! 20 psi? Like has been mentioned, that's a ticking time bomb. Go with the larger waste gate and put a smaller spring and get it retuned. You'll be able to enjoy it a lot longer.
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90 GT 393 5 spd, 467 rwhp 480 rwtq 92 coupe, R/S 308 5 spd 93 coupe, 2.3 5 spd
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#7 |
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I Post Entirely Way Too Much
1991 Ford Mustang GT
Join Date: May 2007
Location: San Diego, California
Posts: 6,063
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great numbers....just be careful, I'm sure you have a lot of money in her, id hate for her to self destruct
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![]() DART 331ci stroker, AFR 185 heads, Trick Flow R intake, Accufab 70mm tb, 75mm pro m Maf, 30lb injectors, jba headers, 2 1/2" x pipe flowmaster super 10 mufflers, 255 fuel pump, 3:27 gears |
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#8 |
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Regular
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20psi on a stock bottom end and block just doesn't sound comforting at all
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#9 |
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Hardcore Enthusiast
1989 Mustang GT 5.0
Join Date: Oct 2007
Location: CT
Posts: 2,186
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Wastegate is too small...shit is garage.. goingto a tial 44mm prolly 10lb spring..cuz i was not happy when i saw 17lbs i never wanted.to boost past 10lbs and i keep blowing off plug wires?
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Cage Maximum Motorsports Sparco QH/BE Nitto "a huge bad azz motor is nice untill you have to turn or stop" |
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#10 |
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I Post Entirely Way Too Much
1991 Ford Mustang GT
Join Date: May 2007
Location: San Diego, California
Posts: 6,063
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^^ How do you blow off plug wires ?
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![]() DART 331ci stroker, AFR 185 heads, Trick Flow R intake, Accufab 70mm tb, 75mm pro m Maf, 30lb injectors, jba headers, 2 1/2" x pipe flowmaster super 10 mufflers, 255 fuel pump, 3:27 gears |
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#11 |
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Hardcore Enthusiast
'89 LX 'Vert
10's or bust... Literally.
Join Date: May 2009
Location: Denver, Co
Posts: 2,915
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lol, they might FALL off, but I doubt they are BLOWING off.
just squeeze them a little with some pliers.
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H/C/I 302 + nitrous for now... supercharger/turbo soon? ![]() |
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#12 |
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MM Fanatic
89 GT
Join Date: Apr 2007
Location: NY
Posts: 4,875
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What, you guys don't know about hollow core sparkplugs?
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#13 |
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Banned
1992 Lx
11.39@119.24
Join Date: Jan 2008
Location: Az
Posts: 11,644
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If my shit gets on the dyno and touches 17 its not doing another pull derp
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[QUOTE=93mustank;2577445]We speed tested my right arm for quickness in shifts... So he could design the cam for proper shift recovery.[/QUOTE] |
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#14 |
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Premium Member
1969 Mustang Mach 1
6.824@101.61
Join Date: Aug 2006
Location: Oklahoma jackass, get to driving
Posts: 5,565
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I don't know about hollow spark plugs, but I just towed my truck home because the POS showed me how to launch a spark plug out of the hole. Fuggin POS modular motors!
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./___ _ ____ ___ \. ( ]]] _ _ O _ _ [[[ ) \_ o _ _____ _ o _/ |___| ......... |___| http://www.youtube.com/watch?v=HyYU3...e_gdata_player |
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#15 |
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Banned
1992 Lx
11.39@119.24
Join Date: Jan 2008
Location: Az
Posts: 11,644
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__________________
[QUOTE=93mustank;2577445]We speed tested my right arm for quickness in shifts... So he could design the cam for proper shift recovery.[/QUOTE] |
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#16 |
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Hardcore Enthusiast
'89 LX 'Vert
10's or bust... Literally.
Join Date: May 2009
Location: Denver, Co
Posts: 2,915
![]() ![]() iTrader: 0 reviews
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lmao, why didn't she just sit down?
would have been epic if she got so scared that she farted, and shot a fire ball in her friends face
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H/C/I 302 + nitrous for now... supercharger/turbo soon? ![]() |
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#17 | |
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MM Fanatic
89 GT
Join Date: Apr 2007
Location: NY
Posts: 4,875
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How the fuck did you pop a plug all the way out of it's threads BTW? |
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#18 |
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Banned
1992 Lx
11.39@119.24
Join Date: Jan 2008
Location: Az
Posts: 11,644
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its a ford thing, the threads come outa the head
__________________
[QUOTE=93mustank;2577445]We speed tested my right arm for quickness in shifts... So he could design the cam for proper shift recovery.[/QUOTE] |
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#19 |
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Hardcore Enthusiast
1989 Mustang GT 5.0
Join Date: Oct 2007
Location: CT
Posts: 2,186
![]() iTrader: 0 reviews
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I meant the plug wire came off the spark plug... soo founds some issues one blew a hose clamp on intercooler piping. Had a vacuum leak car would fall on her face when entering boost. Two my oil feed line is leaking..... three driving in four hours of trafficin ny today i fried the clutch cable on an off ramp amd was stranded for an hour till a nice guy with his excursion towed me to my friends house....just took cable out new one going in tomorrow
__________________
Cage Maximum Motorsports Sparco QH/BE Nitto "a huge bad azz motor is nice untill you have to turn or stop" |
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#20 |
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Premium Member
1969 Mustang Mach 1
6.824@101.61
Join Date: Aug 2006
Location: Oklahoma jackass, get to driving
Posts: 5,565
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Like snatch said. The POS modulars blow plugs out, because they literally have 3 threads that hold the plug in the head. I was sitting at a stoplight, and when it turned green, I touched the gas and BOOM! It blew the plug out. So not only does it rip the threads out of the head, but it ruins a $100 coil pack too. It's a PITA to work on too. I hate modulars.
__________________
./___ _ ____ ___ \. ( ]]] _ _ O _ _ [[[ ) \_ o _ _____ _ o _/ |___| ......... |___| http://www.youtube.com/watch?v=HyYU3...e_gdata_player |
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