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#1 |
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Fashion Guru
Join Date: Jul 2006
Location: Waterville, OH
Posts: 2,039
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Goobers blown engine
i decided just to make a different thread about it.
for those that don't know i blew my engine back in october. i had a vortech v1 at 6psi making 272rwhp/284rwtq and only other mod was exhaust. ![]() ![]() ![]() i pulled out a lot and that is just what is left over that i didn't get. ![]() ![]() ![]() ![]() ![]() ![]()
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#2 |
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Regular
2003 mustang v6
232rwhp@7psi
Join Date: Jul 2007
Location: jackson, MS
Posts: 245
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what happenend? and how did you get 270 rwhp on 6 psi?
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V0rTech'D
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#3 |
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Fashion Guru
Join Date: Jul 2006
Location: Waterville, OH
Posts: 2,039
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i was going down the track and just crossed the finish line and it happened.
i went to a well known guy that deals specifically with mustangs. he is out of Norwalk Ohio, just down the street from Summit Motorsports Park. just read the first page and you will see how easy it was for them to get 272 out of my car CRT Performance |
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#4 |
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Smelly Fists, Socking Cocks
Millenium Falcon
"Lived the Dream, Created the Reality, Basking in my Awesomeness"
Join Date: Mar 2007
Location: Zip's Bubble
Posts: 12,798
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575wrhp out of a KB termi is weak sauce
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#5 |
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[8MINUS2]
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^
Must agree. How did you blow it up? Miles on it? Did you ever post your dyno graph I don't remember if you did or not. Pics with heads off ftw!
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![]() Hi, You can call me Kyle Last edited by ESG-642T; July 2nd, 2009 at 08:40 PM. |
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#6 |
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Fashion Guru
Join Date: Jul 2006
Location: Waterville, OH
Posts: 2,039
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for the last time I DON'T KNOW HOW IT BLEW UP!! maybe you just never read my posts when you asked me that the last 10 times. i had 56,9xx miles on it. i don't have the dyno graph anymore. i threw it away a long time ago since i don't need it
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#7 |
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Enthusiast
1994 Ford Mustang GT
Join Date: Sep 2006
Location: Shawano, WI
Posts: 580
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hmm, pull the heads off and snap some pictures, should be a good starting point as to what went wrong, sucks that you only had 280 and she went
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www.moddedmustangs.com |
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#8 |
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Regular
Join Date: May 2008
Posts: 396
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Can't wait to see pictures once you get the heads off.
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#9 |
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Hardcore Enthusiast
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#10 |
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MM Fanatic
2000 gt
Join Date: Feb 2009
Location: La grange, KY
Posts: 3,982
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i hate that for you. went through it about 2 years ago. but i knew what was up before i pulled a head. 2 sparkplugs smashed completely flat lol.
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Procharged 2000 5 Speed BAB GT, built motor, blower cams, speedy dyno tune 412 hp, 450 rw tqHARDCORE CREW BRIGHT ATLANTIC BLUE CREW #1 MEMBER |
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#11 | |
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[8MINUS2]
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6psi/270hp/56k miles, something went wrong somewhere.
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![]() Hi, You can call me Kyle |
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#12 |
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Safud: MM's Resident Hadji
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Chris torres building the motor
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#13 |
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Hardcore Enthusiast
2003 V6 Mustang
Too long@Too slow
Join Date: Oct 2008
Location: NC
Posts: 2,672
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subscribing
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#14 |
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MM's Resident Ricer
2006 Scion tC
13.001@113
Join Date: Nov 2006
Location: Raleigh/Lenoir, NC
Posts: 9,906
Blog Entries: 2
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what did you end up doing with the car man?
I know you were thinking v8 but i never saw the result
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![]() Scion Tc Turbo - 9psi 297whp 287wtq 2500lbs :p MM 4 Banger club: Senior Ricer NCMM #9 "Horsepower sells cars, torque wins races." -Carroll Shelby |
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#15 |
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Fashion Guru
Join Date: Jul 2006
Location: Waterville, OH
Posts: 2,039
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it was a stock motor so unless chris was working 45 minutes north then no he didn't build the engine
why are you subscribing? it was a stock block that blew because i was too hard on it. thats the only thing i can think of im just gonna put another stock block in it and hopefully sell it and get something better |
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#16 |
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MM's Resident Ricer
2006 Scion tC
13.001@113
Join Date: Nov 2006
Location: Raleigh/Lenoir, NC
Posts: 9,906
Blog Entries: 2
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got ya
__________________
![]() Scion Tc Turbo - 9psi 297whp 287wtq 2500lbs :p MM 4 Banger club: Senior Ricer NCMM #9 "Horsepower sells cars, torque wins races." -Carroll Shelby |
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#17 |
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Hardcore Enthusiast
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wait wait wait...so...how many miles did you have? and how did you blow it up? and how much psi were you running? and...im totally just kidding bro...that does suck....
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![]() 94v6.CAI,Exhaust,3:73s-needs rear end rebuild 02GT/Saleen.built motor,62mm turbo 412hp/446tq @10psi,stock TB and intake |
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#18 | |
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Enthusiast
1994 Ford Mustang GT
Join Date: Sep 2006
Location: Shawano, WI
Posts: 580
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270 on a stock v6 isnt an issue unless you have an issue/s
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www.moddedmustangs.com |
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#19 |
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Hardcore Enthusiast
Join Date: Feb 2007
Posts: 1,181
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The metal that is in the engine looks like it is the remains of a piston. The stock hypereutectic pistons are claimed to commonly fail if pushed too hard. They are an alloy of aluminum and silicon that is hard but somewhat brittle. You might want to rebuild the engine with forged pistons.
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#20 |
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Hardcore Enthusiast
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defective rotating assembly piece?
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